Zhengda Yang,
Chenghang Zheng*,
Xuefeng Zhang,
Qianyun Chang,
Weiguo Weng,
Yi Wang and
Xiang Gao*
State Key Lab of Clean Energy Utilization, State Environmental Protection Engineering Center for Coal-Fired Air Pollution Control, Institute for Thermal Power Engineering, Zhejiang University, 38 Zheda Road, Hangzhou 310027, China. E-mail: zhengch2003@zju.edu.cn; xgao1@zju.edu.cn; Fax: +86-571-87953129, +86-571-87951616; Tel: +86-571-87953129, +86-571-87951335
First published on 2nd January 2018
Eliminating sulfuric acid aerosol from flue gas is of vital importance to improve air quality. In this paper, a wet electrostatic precipitator (WESP) assisted with novel pre-charger was proposed to efficiently remove sulfuric acid aerosol. Parameters including residence time, gas temperature and SO3 concentration were studied to find the key factors influencing sulfuric acid aerosol removal. Results showed that the removal efficiency of sulfuric acid aerosol increased with the increasing residence time and the decreasing gas temperature. The maximum corona current was reduced from 0.79 to 0.28 mA when the SO3 concentration increased from 0 to 25 ppm, and the removal efficiency also decreased with the increasing SO3 concentration. A novel perforated pre-charger was designed to improve the WESP performance for sulfuric acid aerosol removal. With assistance of the pre-charger, the removal efficiency was improved from 90.3 to 95.8%, and the corresponding emission concentration was lower than 2 mg m−3. Moreover, the removal efficiency could be further improved to 97.8% with a heat exchanger, and the corresponding emission concentration could be lower than 1 mg m−3.
In coal-fired power plants, the formation of sulfuric acid aerosol comes from the combination of SO3 with flue gas moisture. During combustion process in the boiler, a part of sulfur in fuels can be oxidized to gaseous SO3. The SO3 concentration increases significantly after selective catalytic reduction (SCR) system because 0.25–1.25% of SO2 can be converted to SO3.1,5,6 When the flue gas enters into the wet flue gas desulfurization (WFGD), the flue gas temperature can be easily quenched to below 50 °C, and correspondingly saturated gas condition is established.7,8 During this process, gaseous SO3 will combine with H2O molecules to form sulfuric acid aerosol. The sulfuric acid aerosol is too small to be efficiently captured by WFGD.5 Heterogeneous vapor condensation method can be used to enlarge the aerosol size and improve the removal efficiency of WFGD. However, the removal efficiency is still less than 70% and the emission of mass concentration is more than 15 mg m−3.9 Once sulfuric acid aerosol is discharged from the stack without further control methods, the stack is typically featured as bluish plume and human health will be endangered particularly when burning high sulfur content coal. As a possible countermeasure, WESP is installed downstream of WFGD to control fine dust particles and carryover of slurry droplets, which can simultaneously eliminate the emission of sulfuric acid aerosol.2
WESP removes fine particles including sulfuric acid aerosols electrostatically with high removal efficiency, and the stack plume condition will be significantly improved. Inside a WESP, flue gas is ionized by high voltage to produce ions and electrons. When sulfuric acid aerosol enters WESP, it is negatively charged as a result of field charging and diffusion charging effects. Field charging is dominant for aerosols larger than 1.0 μm, and diffusion charging contributes more for aerosols less than 1.0 μm.10 The charged aerosols are driven by electric force to move towards collection plates and emerge into liquid film.11–14 The removal efficiency of sulfuric acid aerosol by WESP is much higher than WFGD.15 The removal efficiency increased with the increasing of specific surface area (SCA) and electric field intensity.16 Nevertheless, WESP may suffer with efficiency reduction when dealing with gases with high SO3 concentrations.5 Generally, small size of sulfuric acid mist is the primary factor limiting efficient separation from flue gases. Some agglomeration technologies, i.e., acoustic agglomeration, electrical agglomeration and chemical agglomeration,17–20 are possible solutions to improve fine particle removal efficiency by enlarging particle size. However, all these technologies are only implemented before dry ESP or before WFGD. Additionally, some researchers pointed out that separation efficiency of fine particle can be improved by electrostatic pre-treatment methods. Multi-field WESP is an easiest way to improve the removal efficiency.21 Chang et al. proposed a bipolar charger to agglomerate particles with water droplet humidification.20 Kim et al. developed a novel two-stage WESP which used a carbon brush pre-charger to increase the removal performance for ultrafine particles.22 Their results showed that electrostatic pre-treatment combined with WESP can be a cost-effective method to improve the removal efficiency.
Enhanced methods are widely used to improve fine particle removal efficiency, while mineral work reports on the improvement of WESP performance for sulfuric acid aerosol removal. In this study, a horizontal WESP experimental system was designed to investigate the removal of sulfuric acid aerosol under simulated flue gas condition. The aerosol size distribution was measured to study the sulfuric acid aerosol formation characteristics before WESP. Influences of residence time, gas temperature and SO3 concentration on removal efficiency were investigated experimentally without any enhanced methods. On this basis, a novel perforated pre-charger was carefully constructed to improve removal efficiency of sulfuric acid aerosol. With the assistance of a pre-charger and a heat exchanger, various emission requirements can be satisfied.
The cross section of the WESP was rectangular (120 mm × 300 mm), and the length of the WESP was 1200 mm. The discharge electrode was consisted of 10 wires placed with an interval of 10 mm, and the distance between discharge electrode and collection plate was 60 mm. Two Teflon insulators were used to fix the discharge electrodes in the center of the WESP. To ensure the insulating properties at saturation gas condition, the insulator surface was heated by an electric heater. A high frequency power supply (50 kV, 2 mA, 20 kHz, and negative DC) was connected with the discharge electrode to generate corona ions. A pre-charger was installed at the inlet of the WESP and was configured with spike-wires and two air distribution plates. Another power supply (40 kV, 2 mA, 20 kHz, and negative DC) was connected with the pre-charger to generate strong electric field and produce high density ions.
The contaminated flue gas was simulated by introducing SO3 into main gas stream. A fan was used to provide the main gas with maximum flow rate of 140 m3 h−1. An electric heater with maximum electric power of 20 kW was used to heat the air to set temperatures (90–120 °C). An S-type thermal couple was installed at the exit of the electric heater to measure the gas temperature and fed back the temperature to the controller to adjust the heating power. All gas pipes were covered with thermal insulation material to reduce heat loss. The hot gas was scrubbed by a WFGD tower, resulting in significant drop of gas temperature to about 45 °C. Consequently, a saturation, or even super-saturation gas condition pre-existed before entering the WESP.
SO3 was produced by an SO3 generator and was completely converted to sulfuric acid aerosols by nucleation during WFGD process. The SO3 generator worked on the principle of SO2 oxidation catalyzed with vanadium pentoxide (V2O5). The catalyst reactor was maintained at approximately 410 °C to promote SO3 conversion efficiency. An SO2 gas analyzer was used to measure the SO2 concentration, and the conversion efficiency from SO2 to SO3 was supposed to be as high as 100% since no residual SO2 was detected at the exist of the generator.
Sulfuric acid aerosol is fine droplet of sulfuric acid solution. It cannot be measured with off-line weighing method by collecting it on impactors or films. An on-line device of electrical low pressure impactor (ELPI+, Dekati Ltd., Finland) was used to measure the concentration of sulfuric acid aerosol with different diameters. It works on the principle of induced current method. The aerosol is charged to known charge level in a unipolar corona charger and then classified into different stages depending on aerosol diameters. The current on each stage is detected by sensitive electrometer, the signal of which is inverted to calculate aerosol number concentrations. The sampling gas flow rate of the ELPI+ is 10 L min−1, generated by a vacuum pump. The number concentration of sulfuric acid aerosol can be higher than 1 × 108 cm−3, and a diluter (Diluter DI-1000, Dekati Ltd., Finland) was used to dilute the gas with clean air. Reducing gas temperature can lead to the growing of sulfuric acid aerosol by condensation, thus the probe was heated to the same temperature with the flue gas to ensure the sampling accuracy.
The WESP performance for the removal of sulfuric acid aerosol was evaluated by the fractional and total removal efficiencies, which can be calculated by the following equations, respectively:
(1) |
(2) |
Fig. 2 Size distribution of sulfuric acid aerosol: (a) concentration evolution and (b) fractional concentration at inlet/outlet of WFGD. |
Dust removal efficiency usually increases as the inlet dust concentration increased,25,26 while the removal efficiency of sulfuric acid aerosol presented completely different results with similar concentration loadings as shown in Fig. 7. The removal efficiency of sulfuric acid aerosol decreased with the increasing SO3 concentration. As an example, when the applied voltage was 32 kV, the removal efficiency dropped from 91.0 to 87.3% with the SO3 concentration increasing from 5 to 25 ppm. The difference can be larger for lower applied voltage, and the removal efficiency dropped from 33.6 to 7.1% when the applied voltage was 16 kV. This phenomenon can be explained by the relationship between the corona discharge and particle charging. The above-mentioned corona current decreased with the increasing SO3 concentration, indicating the ion density in space decreased in the presence of SO3. Our previous numerical work23 showed that the negative influence on the removal of sub-micron particle was more noticeable when reducing ion current. In industrial application, some WESPs can experience very high SO3 concentrations when dealing with high sulfur content fuels. These WESPs can be less effective, thereby some improvements were needed to improve the removal efficiency of sulfuric acid aerosol.
Flue gas was introduced into the pre-charger and thus sulfuric acid aerosol was negatively charged before entering the WESP. The pre-charger was primarily used for aerosol charging and the WESP was primarily used for aerosol collection. In the pre-charger, the distance from pin to plate was 25 mm, which was much shorter than that in the WESP. Fig. 9 presents current–voltage characteristics of the pre-charger and the WESP. Similarly, the corona current of the pre-charger decreased significantly in the presence of SO3 (Fig. 9a), while the corona current of the WESP increased with the increasing pre-charger voltage (Fig. 9b). When aerosols passed through the pre-charger, they were charged and partly collected. That is, with the assistance of pre-charger, corona suppression mainly occurred in the pre-charger, and the corona discharge of WESP was significantly improved. Compared with the WESP, the current density on the perforated plates of the pre-charger was much higher. The maximum current densities were 16.03 and 0.45 mA m−2 respectively for the pre-charger and the WESP when the SO3 concentration was 10 ppm.
Removal efficiencies of sulfuric acid aerosol under different pre-charger voltages are shown in Fig. 10. The performance of WESP was not good under low applied voltages, but the removal efficiency was significantly improved with the assistance of pre-charger. As an example, when the WESP voltage was 16 kV, the removal efficiency increased from 27.9 to 82.4% as the pre-charger voltage increased from 0 to 16 kV. The key reason was that the pre-charger provided sufficient ions for aerosol charging even though the WESP operated under low applied voltage. The removal efficiency can be as high as 95.8% when the pre-charger and the WESP both operated under maximum applied voltages. The WESP and combined WESP (WESP + pre-charger) are compared in Table 1. For the WESP only, increasing SCA can achieve the same removal efficiency with the combined WESP. Namely, the overall SCA can be reduced by using the pre-charger. As an example, the overall SCA was reduced from 28.80 to 22.27 m2 (m3 s−1)−1 when the pre-charger voltage was 8 kV.
Furthermore, the fractional removal efficiencies of sulfuric acid aerosol with pre-charger on and off are compared in Fig. 11. The fractional removal efficiency curves had similar tendencies for the two cases. For aerosols with diameter less than 0.03 μm, the removal efficiency decreased significantly with the decreasing aerosol diameter. For aerosols with diameter larger than 0.03 μm, there existed a minimum removal efficiency for aerosols with diameters about 0.1 μm. This phenomenon was attributed to the size dependence of particle charging and electrical mobility. Inside an ESP, particles are charged by field charging and diffusion charging effects. Field charging is dominant for particles larger than 1.0 μm and diffusion charging is dominant for particles smaller than 0.1 μm, respectively.10 The electrical mobility for aerosols with diameters about 0.1 μm was small because of the two charging effects, which accounts for the minimum removal efficiency in this size range. For particles smaller than 0.03 μm, some of them cannot be charged due to the partial charging effect, resulting in a decrease of collection efficiency.27 The WESP performance for removal of sulfuric acid aerosol was improved assisted with pre-charger. The improvement is more noticeable for aerosols in the range from 0.03 to 0.5 μm because the substantial increase of electrical mobility in this range.
A heat exchanger was installed downstream the WFGD to further improve the removal efficiency of sulfuric acid aerosol since the removal efficiency was influenced by flue gas temperature. With the application of heat exchanger, the gas temperature could be cooled down from 43.2 to 39.1 °C. Removal efficiencies and emissions of sulfuric acid aerosol in three operation cases are compared in Fig. 12. The sulfuric acid aerosol was removed by WESP with an efficiency of 90.3%, and the efficiency was improved to 95.8% assisted with pre-charger. Moreover, the removal efficiency could be further improved to 97.8% assisted with pre-charger and heat exchanger at the same time. As can be seen from Fig. 12, emissions of sulfuric acid aerosol can reach different levels in different cases. In case 2, the emission concentration of sulfuric acid aerosol was lower than 2 mg m−3, and it could be lower than 1 mg m−3 in case 3 with the assistance of pre-charger and heat exchanger. In real application, technologies can be determined based on the emission requirements of sulfuric acid aerosol.
Fig. 12 Comparison of sulfuric acid aerosol removal for different cases (case 1: WESP, case 2: WESP + pre-charger, and case 3: WESP + pre-charger + heat exchanger). |
This journal is © The Royal Society of Chemistry 2018 |