Yuqiu Hou,
Mei Liu,
Xiao Tan,
Siyu Hou and
Ping Yang†
*
College of Architecture and Environment, Sichuan University, Chengdu 610065, China. E-mail: yangpinga301@163.com; 740659077@qq.com; 707865212@qq.com; heishihe@163.com; 240736328@qq.com; Tel: +86 18602804508
First published on 10th August 2021
A moving bed biofilm reactor (MBBR) is a kind of commonly used biological sewage treatment process. A carrier, the core of MBBR, could directly affect the treatment efficiency of MBBR. In this experiment, a hybrid carrier composed of an MBBR carrier and fluidized bed porous carrier was innovatively utilized to treat low-concentration simulated domestic sewage through an MBBR reactor to investigate the effects of different hydraulic retention times (HRT) and different carrier dose ratios on the reactor performance. The results indicated that when the volume ratio of the carrier dosage was 5%:20% when the reactor HRT was 5 h, the removal rates of ammonia nitrogen, total nitrogen (TN) and chemical oxygen demand (CODCr) were optimal, which were 96.5%, 60.9% and 91.5%, respectively. The ammonia nitrogen, total nitrogen and CODCr concentrations of the effluent were 1.04 mg L−1, 12.20 mg L−1 and 29.02 mg L−1, respectively. Furthermore, the total biomass concentration in the hybrid carrier biofilm reactor (HCBR) was 3790.35 mg L−1, which also reached the highest value. As the experiment progressed, the concentrations of protein, polysaccharide and soluble microbial products (SMP) were reduced to 7.68 mg L−1, 11.10 mg L−1 and 18.08 mg L−1, respectively. This was basically consistent with the results of the three-dimensional fluorescence spectrum. The results showed that the combined-carrier biofilm reactor could reduce the volumetric filling rate, improving the removal capability of organic matter and the denitrification efficiency. This study provided technical support for the composite carrier biofilm wastewater treatment technology, and also had a good prospect of application.
The MBBR method was developed in 1988 by the Norwegian Kaldnes company, and the Norwegian University of Science and Technology and the SINTEF research institute. The core of this process was directly adding the suspended filler with a specific gravity close to water into the aeration tank as a carrier for microbial adhesion growth. The MBBR method combines the advantages of the activated sludge method and the biofilm method, including small floor area, no need for sludge reflux or backwashing, low head loss, low power consumption, and high resistant to temperature changes and changes in sewage composition. Moreover, the treatment capacity of sewage has been improved, and the nitrification effect also has been significantly enhanced. In the past few decades, the MBBR process has been employed worldwide.3,4 It has been applied in treating urban domestic sewage,3,5,6 food industry wastewater,7 papermaking wastewater8 and landfill leachate.9,10 In recent years, the MBBR method was also suggested for the treatment of pharmaceutical wastewater11 and phosphorus removal.12,13
The biological fluidized bed method is a sewage treatment process developed in the early 1970s. Its principle is to use small inert porous particles, such as activated carbon, as carriers to degrade the aerobics of pollutants in wastewater. The microorganisms were immobilized on the surface of the carrier, and the carrier was fluidized to degrade the contaminants in the wastewater.14 Until now, biological fluidized bed reactors have been developed in various forms. They were also widely studied and applied in urban domestic sewage,15 industrial wastewater14 and landfill leachate.16
The integrated fixed-film activated sludge (IFAS) method integrates the hybrid biofilm process and activated sludge process to treat sewage.17 The bacterial richness and microbial diversity in biofilms and flocs of the IFAS system were different, which would promote high microbial diversity to achieve higher pollutant removal efficiency.
Carrier research is an important direction for the development of the biofilm process.18 Commonly used carrier materials can be divided into inorganic carrier materials, natural organic carrier materials, synthetic polymer carrier materials and composite carrier materials, according to their properties. With the objective to act as an effective support media for active biomass growth in a biofilm reactor, the ideal carrier material should have several desirable characteristics. Optimally, carriers should (i) have good compatibility with microorganisms and will not affect the biological activity of the microorganisms, (ii) be environmentally friendly, biodegradable, and will not cause secondary pollution, (iii) shield unfavorable external environmental conditions, provide carbon sources, nutrients and a good microenvironment, (iv) have a relatively large specific surface area; raw materials are easily available and low in price, (v) have good stability and can be used for a long time or repeatedly.19 The specific surface area, pore structure, mechanical strength and other factors of different carrier materials will significantly affect the immobilization process of microorganisms.20 A suitable carrier can improve the sewage treatment capacity. According to a previous study, in addition to polyethylene (PE), polypropylene (PP), and high-density PE (HDPE), polymers such as polyurethane (PU) and polycaprolactone (PCL) have been used as biofilm carriers in MBBRs.21 Among these, biofilm carriers composed of PE are often used in MBBRs because the density of PE is lower than that of other polymers.22 Moreover, polyethylene terephthalate (PET), produced from waste plastic bottles, can be utilized as a packing material for up-flow anaerobic sludge bed (UASB) reactor as demonstrated by M. A. EI-Khateeb.23 The quality of the packed UASB (P-UASB) effluent was found to be better than that of the classical UASB reactor.23 What is more, the down flow hanging non-woven (DHNW) reactor packed with PET has achieved excellent performance in the treatment of tanning effluents.24 Abu Bakar used two types of biofilm carriers to fill the MBBR to treat palm oil mill effluent. The results indicated that the hexafilter performed better than black plastic media at 50% media filling fractions (retention time of 72 h).21 Theoretically, the mixed-carrier biofilm reactor can simultaneously take advantage of the advantages of the two carriers and make up for each other's defects, which will greatly promote the improvement of the processing efficiency of the biofilm reactor. However, there are few research studies on mixed carrier biofilm reactors at home and abroad.
Based on this, the experiment quoted the method of IFAS, combining the MBBR carrier and the fluidized bed carrier into a combined-carrier. The simulating domestic sewage was processed through the MBBR reactor, and the influence of different HRT and carrier dosage ratios is discussed on the performance of the reactor.
Parameters | BioM™ carrier | Parameters | Porous polymer particle carrier |
---|---|---|---|
Type | WD-F10-4 | Dry particle size (mm) | 0.45–0.90 |
Size (mm) | Φ10 × 10 | Skeleton density (kg m−3) | 1320.00 |
Surface area (m2 m−3) | 1200.00 | Wet bulk density (kg m−3) | 1010.00 |
Packing number (m−3) | 495000 | Vacancy capacity (mL g−1) | 0.301 |
Packing density (kg m−3) | 125.00 | Wet surface area (m2 m−3) | 5357.00 |
Pre-film density (g cm−3) | 0.96–0.98 | ||
Post-film density (g cm−3) | 1.00 |
Nutrient solution A | Concentration (g L−1) | Nutrient solution B | Concentration (g L−1) |
---|---|---|---|
FeSO4·7H2O | 6.985 | NiCl2·6H2O | 0.250 |
MnSO4·H2O | 1.067 | (NH4)6Mo7O24·4H2O | 0.125 |
ZnSO4·7H2O | 0.263 | H3BO7 | 0.125 |
CoSO4·7H2O | 0.443 | CuCl2·2H2O | 0.075 |
The measurement of the attached biomass on the BioM™ carrier was measured by the lye dissolution spalling method.25 Five randomly selected BioM™ carriers were charged into the reactor, dried at 105 °C to a constant weight, and then weighed. Then, the carriers were placed in a 0.1 mol L−1 NaOH solution and heated to 60 °C for 20 minutes. The degree of bonding between the biofilm and the carrier surface was greatly reduced, and the biofilm on the carrier was peeled off mechanically to remove water. The carriers were washed and dried at 105 °C to a constant weight, and then weighed. The total weight of the attached biomass on the carriers was calculated and converted to the biomass concentration of the attached biofilm on the BioM™ carrier throughout the reactor.
The amount of attached biomass on the porous polymer particle carrier was determined by the microscopic test diameter density calculation method. Boaventura et al.26 and Coelhoso et al.27 found that the density of the biofilm attached to the biofilm carrier was related to its thickness. When the thickness of the biofilm was less than a certain value, the density of the biofilm decreased linearly with the increase of the thickness. Moreover, when the film thickness increased to a certain value, the density of the biofilm no longer changed with the increase of the film thickness. The biofilm density ρ fitted by Boaventura et al.28 through experimental data was calculated by the following eqn.
ρ (mg cm−3) = 104.3 − 0.224LL < 622 μm | (1) |
ρ (mg cm−3) = 26.9L > 622 μm | (2) |
The thickness L of the biofilm adhered to the porous polymer particle carrier was measured by referring to the experimental method of Pan et al.29 The irregular porous polymer particle carrier was regarded as an ellipsoid, and the long axis a of the ellipsoid was measured by an optical microscope. The short axis b was converted into the equivalent sphere diameter d = (a·b2)1/3. In each test, 100 carrier particles were randomly selected from the reactor for testing. The average diameter of Sauter was used to represent the average diameter of 100 carrier particles De = ∑d3/(∑d2). In addition, 100 optical carrier particles were selected in the same way to test the average diameter Dc = 1351.66 μm, the volume V0 = 1.293 mm3, and the biofilm thickness L is (De − Dc)/2. After the biofilm density ρ was obtained according to the thickness of the biofilm, the biofilm volume was determined: Finally, the biomass concentration of the biofilm was X = ρV.
Carrier ratio | HRT (h) | Volume loading | ||
---|---|---|---|---|
kg COD (m3 d)−1 | kg NH3–N (m3 d)−1 | |||
P1 | 2%:20% | 11 | 0.87 | 0.076 |
8 | 1.2 | 0.105 | ||
5 | 1.92 | 0.168 | ||
2.5 | 3.84 | 0.42 | ||
P2 | 5%:20% | 2.5 | 3.84 | 0.42 |
5 | 1.92 | 0.168 | ||
8 | 1.2 | 0.105 | ||
11 | 0.87 | 0.076 | ||
P3 | 8%:20% | 11 | 0.87 | 0.076 |
8 | 1.2 | 0.105 | ||
5 | 1.92 | 0.168 | ||
2.5 | 3.84 | 0.42 |
C6H12O6 + 6O2 → 6CO2 + 6H2O | (3) |
The removal of CODCr during the experiment is shown in Fig. 3. Under different carrier ratios, the CODCr removal effect of the reactor was almost flat. When the HRT were 5 h, 8 h and 11 h, the average effluent CODCr of the reactor was about 30 mg L−1, and the average CODCr removal rate was about 90%. When the HRT was 2.5 h, the CODCr removal rate of the reactor decreased slightly, and the effluent CODCr concentration increased slightly. The average concentration was 45.2 mg L−1, and the average removal rate was about 87%. In the 12 working conditions of the experiment, when the carrier ratio was 2%:20% and the HRT was 5 h, the average effluent CODCr of the reactor was 22.89 mg L−1 and the average removal rate of CODCr was 93%. That was optimal processing efficiency.
The results indicated that the carrier ratio had little effect on the CODCr removal effect of the HCBR. The removal rate of CODCr was positively correlated with the change of HRT.32 This change may due to the fact that different HRTs would cause the F/M in the reactor to be different.33 The shorter the HRT was, the larger the F/M was. Meanwhile, the carrier provides a stable growth environment for microorganisms, thus improving the degradation effect of the reactor.34 However, when the loading was so high that the microorganisms in the reactor could not degrade the organic matter in time, this resulted in a decrease of the CODCr removal rate. When the HRT was prolonged, the microorganisms attached to the carriers would have enough time to contact the organic matter and remove it.32 However, in this experiment, the change of the CODCr removal rate with HRT changes was not prominent, which indicated that the HCBR had a wide load range and strong impact resistance.
2NH4+ + 3O2 → 2NO2− + 2H2O + 4H+ | (4) |
2NO2− + O2 → 2NO3− | (5) |
The degradation of NH4+–N during the experiment is shown in Fig. 4. When the ratios of the carrier dosage were 5%:20% and 8%:20%, the removal rate of NH4+–N in the whole process of the reactor was higher than the removal rate when the dosage ratio was 2%:20%. Furthermore, when the ratios of the carrier dosage were 5%:20% and 8%:20%, the removal rates of NH4+–N were not significantly different from each other. After the reactor stabilized, when HRT was 5 h, the removal rate of NH4+–N was optimal with the dose ratios of 5%:20% and 8%:20%. The average NH4+–N effluent was 1.10 mg L−1 and 0.99 mg L−1, and the removal rates were 96% and 97%, respectively. When the HRT was 2.5 h, the effluent NH4+–N removal rate was less than 90%. Moreover, when the carrier dosage ratios were 5%:20% and 8%:20%, the effluent NH4+–N concentration was 5 mg L−1 ± 1 mg L−1. When the HRT were 8 h and 11 h, the removal rate of NH4+–N in the reactor was above 90%, which was slightly lower than the removal rate of 5 h HRT.
The results indicated that different carrier dosage ratios and different HRT both had effects on the removal of NH4+–N. The reason may be that there was less space for microorganisms to attach on the carrier to generate biofilm in the reactor when the carrier dosage ratio is 2%:20%, resulting in less microbial biomass in the reactor and low removal rate of NH4+–N. However, when the ratio of the carrier was 8%:20%, the removal rates of NH4+–N was not higher than the removal rates when the carrier dosage ratio was 5%:20%. It may be because the excessive carrier filling rate also means the collision between the carriers frequently increased, resulting in an increase in the rate of biofilm desorption on the surface of the carrier.36 Therefore, the amounts of microorganisms in the reactor would not increase greatly with the increase of the carrier ratio, and the removal rate of NH4+–N. The change of HRT had a great influence on the efficiency of NH4+–N removal in the reactor.37 The removal rate of NH4+–N would decrease rapidly by shortening the HRT,38 and the removal rate of NH4+–N would increase significantly by increasing the HRT. The reason may be that the excessive HRT leads to a decrease in the organic load in the reactor, which in turn reduced the microbial metabolic activity39 and the removal rate of NH4+–N. At the same time, the increase of the amount of the porous carrier was beneficial to the removal of NH4+–N, while the effect was not very obvious.
6NO3− + 2CH3OH → 6NO2− + 2CO2 + 4H2O | (6) |
6NO2− + 3CH3OH → 3N2 + 3CO2 + 3H2O + 6OH− | (7) |
The degradation of TN during the experiment is shown in Fig. 5. When the HRT was 11 h or 8 h, 2%:20% of the carrier dosage ratio was more superior. The average TN removal rate at this time was 50%. In contrast, when the HRT was 2.5 h or 5 h, 5%:20% and 8%:20% of the carrier dosage ratios were better. Furthermore, 5%:20% of the carrier dosage ratio was better than 8%:20% of the carrier dosage ratio. When the carrier dosage ratio was 5%:20% and the HRT was 5 h, the TN removal rate of the reactor was optimal. The average effluent TN concentration was 12.20 mg L−1, and the average removal rate was 61%. The possible reason for this difference was that the amounts of microorganisms in the reactor was small when the carrier dosage ratio was 2%:20%. Furthermore, when the organic load was low, fewer microorganisms were just able to digest organic matter over a long HRT. However, it was difficult for the microorganisms to completely degrade organic matter in the reactor when the organic load was high, so the TN removal rate was not very good in this situation. However, when the carrier dosage ratios were 5%:20% and 8%:20%, the amount of microorganisms in the reactor was larger, and the ability to decompose organic matter was stronger. Furthermore, the carrier dosage ratio at 5%:20% was better than 8%:20%. It was probable that when the ratio of the carrier dosage was 8%:20%, the carriers in the reactor were more likely to collide with each other. This affected the adhesion of the biofilm outside the carrier,36 which in turn affected the removal rate of TN in the reactor. The change of HRT also had a great influence on the removal rate of TN.41 When the HRT was too short, the nitrogen in the sewage and the microorganisms on the biofilm would be sufficiently contacted, which also increased the organic load in the reactor and weakened the stability of the biofilm.42 However, when the HRT was too long, the amount of organic matter in the reactor would decrease,39 and the microbial metabolic activity would decrease, which also affected the removal rate of TN.
The change in the attached biomass on the porous polymer particle carrier under different operating conditions of the reactor is shown in Table 4. When the ratio of the carrier dosage was 5%:20%, the biomass attached to the porous polymer particle carrier was more than 8%:20% carrier dosage ratio under each HRT. The reason for this phenomenon may be due to excessive carrier. The probability of collision with each other during the movement of the reactor would increase, and the microorganisms attached to the carrier would fall off during the collision.36 At the same time, with the shortening of the HRT, the biomass attached to the porous carrier under both dosing ratios tended to increase. This might be owing to the HRT shortened so that the organic load increased, which in turn led to a faster growth of biomass.46
Dosage | 2.5 h | 5 h | 8 h | 11 h | |
---|---|---|---|---|---|
Particle size (μm) | 0.375 L | 1454.59 | 1451.27 | 1436.57 | 1422.07 |
0.6 L | 1446.25 | 1445.64 | 1428.40 | 1411.73 | |
Film thickness (μm) | 0.375 L | 51.46 | 49.81 | 42.46 | 35.20 |
0.6 L | 47.30 | 46.99 | 38.37 | 30.04 | |
Density (mg cm−3) | 0.375 L | 97.89 | 98.10 | 99.01 | 99.92 |
0.6 L | 98.41 | 98.45 | 99.52 | 100.56 | |
Biomass (mg L−1) | 0.375 L | 1682.76 | 1628.13 | 1385.97 | 1147.64 |
0.6 L | 1545.43 | 1535.39 | 1251.72 | 978.18 |
Comparing Fig. 7 with Table 4, the attached biomass of the porous polymer particle carrier was generally higher than the BioM™ carrier. When the HRT was 2.5 h, the organic load was high and the attached biomass on the BioM™ carrier was affected and reduced, while the attached biomass on the porous polymer carrier still maintained an increasing trend. This indicated that the porous polymer particle carrier had a better microbial immobilization effect than the BioM™ carrier. The reason is that the porous polymer particle carrier has a porous structure and good permeability. The microbial flora could be simultaneously attached to the surface of the carrier and the internal pores. This porous structure can significantly increase the degree of microbial aggregation, and facilitate both the metabolism of microorganisms and the diffusion of metabolites, thereby increasing the immobilization effect of the carrier on microorganisms.47
The variation of sludge concentration under different working conditions is shown in Fig. 7. As the ratio of the carrier dosage increased, the sludge concentration in the reactor first increased and then decreased. When the carrier ratio was 5%:20% and the HRT was 5 h, MLVSS reached highest, which was 1273.33 mg L−1. Under different HRT, the MLVSS/MLSS value showed a low trend in the middle. That is, MLVSS/MLSS was higher when the HRT was longer or shorter. However, the activity of the suspended sludge in the reactor was generally low, and the MLVSS/MLSS was kept at about 0.5. Since this experiment mainly studied the attachment of biofilm on the carrier, the change of the concentration of the suspended sludge in the reactor was not considered as the key analysis.
The results are shown in Table 5. When the ratios of carrier dosage were 5%:20% and 8%:20%, the total biomass in the reactor increased with the HRT approaching 5 h. The total biomass in the reactor reached the highest when the HRT reached 5 h. It was speculated that this phenomenon was due to the increasing hydraulic shear caused by too short HRT.43 Hydraulic shearing had a great influence on the peeling of biofilms.48 Excessive hydraulic shearing could increase the difficulty of attaching and fixing microorganisms to the carrier.44 However, if the HRT was too long, the organic load in the reactor would decrease, which may affect the increase of the amount of biomass attached. Moreover, the biomass at 5%:20% of the carrier dosage ratio was more than 8%:20%, indicating that the growth of microorganisms in the reactor would be affected if the carrier dosage ratio was too high.
Carrier dosage ratio | 2.5 h | 5 h | 8 h | 11 h | |
---|---|---|---|---|---|
Biomass (mg L−1) | 2%:20% | 1837.40 | 1572.72 | 1697.95 | 2119.61 |
5%:20% | 3473.04 | 3790.35 | 2763.34 | 2706.51 | |
8%:20% | 2882.02 | 2939.77 | 2748.79 | 2243.67 |
When the carrier dosage ratio was 2%:20%, the change of total biomass in the reactor was exactly opposite. When the HRT was 2.5 h or 11 h, the biomass in the reactor was significantly higher. The reason for this phenomenon was presumed to be that the carrier dosing ratio was too low, and the total biomass was mainly derived from the biomass attached to the BioM™ carrier.
The main components of SMP mainly included proteins, polysaccharides, humic acids, nucleic acids, antibiotics, organic acids, and others.52 Most of them were fluorescent substances. Proteins and polysaccharides were the main ingredients that were ubiquitous in a variety of different situations.53 In this experiment, proteins, polysaccharides and the characteristic peaks of their three-dimensional fluorescence spectra were used simultaneously as indicators to indicate SMP.
Secretion of SMP was found to increase during stress conditions,54 and excessive SMP would have a negative impact on the reaction.55 The SMP concentration of the initial effluent changed greatly, presumably due to the effect of the previous high-salt wastewater degradation experiment on the microorganisms in the reactor before the start of the experiment. In the middle and late stages of the experiment, the SMP concentration in the effluent of the reactor was greatly reduced and it became relatively stable with the change of HRT, indicating that the microorganisms in the reactor have adapted to the influence of the change of the hydraulic conditions, and it could adapt well under each HRT. With the increase of the ratio of carrier dosage, the SMP concentration in the effluent decreased slightly in a stepwise manner, demonstrating that the addition of the porous polymer carrier had less influence on the microorganisms in the reactor.
The change is shown in Fig. 9. It could be found that under different working conditions, the change of the fluorescence intensity of each characteristic peak with time is similar to the change of the sum of protein and polysaccharide in Fig. 9. In the P1 stage, i.e., when the carrier dosage ratio was 2%:20%, the sum of the fluorescence intensities of the organic substances varied depending on the HRT. When the HRT was 5 h, the sum of the characteristic fluorescence intensity of each organic matter was the lowest, which indicated that the HRT of 5 h was the optimum operating condition for reducing the SMP of the water at this stage. In the P2 stage, i.e., when the carrier dosage ratio was 5%:20%, the characteristic fluorescence intensity of each organic substance in the effluent of the reactor also changed greatly with the change of the HRT. When the HRT was 8 h, the sum of the characteristic fluorescence intensities of each organic matter was the lowest, which indicated that the HRT of 8 h was the optimum operating condition for reducing the SMP of the water at this stage. In the P3 stage, i.e., when the carrier dosage ratio was 8%:20%, the characteristic fluorescence intensity of each organic matter changed little with the change of HRT, and the concentration of effluent SMP did not change substantially with the change of HRT. This indicated that at this stage, the microbial system in the reactor was relatively mature, and the load-resistance ability was greatly improved. When the HRT was 5 h, the sum of the characteristic fluorescence intensity of each organic matter was the lowest, indicating that the HRT of 5 h was the optimum operating condition for reducing the SMP of the effluent at this stage.
When the HRT was 5 h in the P1 phase and the HRT were 2.5 h and 5 h in the P2 phase, the B peak representing humus appeared in the spectrum, which was completely different from the effluent under other HRTs. It indicated that the pollutant degradation pathway of the microbial system in the reactor changed at this stage due to the change of HRT, which resulted in a large change in the proportion of components in the effluent SMP. In other cases, the sum of the fluorescence intensities of the characteristic peaks was strong, which manifested that the activity of the microorganisms was stimulated at this time, resulting in an increased secretion in the effluent SMP to alleviate the environmental stress. The sum of the characteristic fluorescence intensities of the organic matter in the P3 stage was generally small. The change with the change of the HRT was also not obvious. It implied that at this stage, the microbial system in the reactor was relatively mature. The load-resistance ability was greatly improved, and the degradation pathway of pollutants was relatively stable.
Footnote |
† Postal address: A301, College of Architecture and Environment, Sichuan University, Chengdu, 610065, China. |
This journal is © The Royal Society of Chemistry 2021 |