Mengjing Caoab,
Yongxiang Zhangab and
Yan Zhang*ab
aFaculty of Architecture, Civil and Transportation Engineering, Beijing University of Technology, Beijing 100124, China. E-mail: yzhang@bjut.edu.cn; Tel: +86 13693219897
bKey Laboratory of Beijing for Water Quality Science and Water Environment Recovery Engineering, Beijing University of Technology, Beijing 100124, China
First published on 22nd September 2021
A novel and amplifying anaerobic electrochemical membrane bioreactor (AnEMBR, R2) was constructed and operated for a long time (204 days) with synthetic glucose solution having an average chemical oxygen demand (COD) of 315 mg L−1, at different applied voltages and room temperatures. More than twice sodium bicarbonate was added for maintaining a pH of around 6.7 in the supernatant of the reactor R2, close to that of a control reactor called anaerobic membrane bioreactor (AnMBR, R1), after 138 days. And the transmembrane pressure (TMP) for the R2 system was only 0.534 bar at the end of operation and 0.615 bar for the R1 system. Although the electrostatic repulsion force contributed to pushing away the pollutants (proteins, polysaccharose and inorganic salt deposits, and so on), more microorganisms adsorbed and accumulated on the membrane surface after the whole operation, which might result in a rapid increase in membrane filtration resistance in the long-term operation. There were much more exoelectrogenic bacteria, mainly Betaproteobacteria, Deltaproteobacteria and Grammaproteobacteria, on the cathode and the dominant methanogen Methanothrix content on the cathode was three times higher than the AnMBR. The study provides an important theoretical foundation for the application of AnEMBR technology in the treatment of low organic strength wastewater.
Integrating microbial fuel cell (MFC) with AnMBR has been proved to be an effective fouling control strategy by reducing particle zeta potential and the amount of SMP in the cathodic mixed liquor.12 But there are two main difficulties for wide application of the MFC system. On one hand, it is difficult to remain the same power densities in the practical engineering application as that in the laboratory system.13 On the other hand, the stability of large bioelectrochemical systems is poor for a long-term operation.13 These problems have been turned out to be closely related to the cathode inevitable biofilm.14 The biofilm growth resulted in increasing fouling of the cathode outer surface.15 And salt deposition, humic acid adsorption and microbial by-products were formed into internal pollutants on the cathode.16–18 Fortunately, a novel anaerobic electrochemical membrane bioreactor (AnEMBR) was developed by Katuri et al. firstly.19 The stability of cathode was enhanced strongly by regulating the applied voltage and the membrane biofouling was mitigated, which could be due to a combination of factors (hydrogen bubble formation, low cathode potential and pH) in this system.19 But there are many problems to be solved in the AnEMBR research filed now.
Metal materials were usually adopted directly as the cathode unit, not environment-friendly products.19,20 Katuri et al. incorporated an electrically conductive nickel-based hollow fiber membrane (Ni-HFM) as the basic separation unit in an AnEMBR system.19 But metal ions in metal membrane might flow into the water through hydraulic-action or ion-exchange and result in potential environmental risk.21 The physical, chemical and biological properties of sludge on the membrane surface may be changed by applied voltage.22,23
The conductive hollow fiber membrane prepared by carbon nanotubes as a basic separation and cathode overcame above problems.21 The good performance of the carbon nanotubes hollow fiber membrane was attributed to high mechanical strength, good hydrophilic characteristics, large specific surface area and encouraging electrical conductivity of carbon nanotubes.24 And Yang et al. found that the carbon nanotubes hollow fiber membrane with negative electro-assistance mitigated membrane pore blocking in the AnEMBR.21 There are two main reasons to suppress the membrane fouling in the AnEMBR system. Increased biogas was produced on the membrane surface, which was similar to a weak gas sparging; less pollutants, especially EPS, were adsorbed and accumulated on the membrane surface because of like electrostatic repulsion between conductive membrane surface and active sludge. But the current studies about the AnEMBR system mainly stay in laboratory-scale system, and with small size. Namely, the reactors were usually small, had a working volume of <1 L or 1 L, and the reactors were operated for <100 days.19,21,25 Hence, it is necessary to explore the performance and membrane fouling control mechanisms of the larger AnEMBR system for a long-term operation, especially, to observe the complicated relationship between the applied voltage and the increased rate of membrane fouling, and compare the differences with the small AnEMBR system.
To address these objectives, an amplifying anaerobic electrochemical membrane bioreactor (AnEMBR) was constructed firstly by the modified polyvinylidene fluoride (PVDF) hollow fiber membrane by coating with multiwalled carbon nanotubes (HF-PVDF-CNT) as the basic separation unit and cathode simultaneously. The operation conditions (pH, temperature, oxidation–reduction potential, and dissolved oxygen) were online monitored to analyze the specific factors and conditions during the whole long-term experiment. The membrane fouling propensity was detected continuously in terms of transmembrane pressure (TMP). The organic, inorganic and physicochemical characteristics, CH4 production and microbial communities were observed for exploring antifouling mechanism in a long-term operation, especially analyzing the difference with the small AnEMBR system.
Moreover, the supernatant pH values remained relatively stable following adding a quantitative NaHCO3 during the whole operation in the reactor R1 (Fig. 1), even tended to increase slightly. In the reactor R2, initial buffered medium contained the same compositions as the reactor R1. But the serious acidification was in the presence of the reactor R2 at 100 days. The supernatant pH values decreased rapidly within 100–114 days, and stabilized at a lower level within 115–125 days. The supernatant in the AnEMBR (R2) acted for liquor in the cathode chamber of the microbial electrolysis cell (MEC). So, acidification could be caused by the accumulation of excess protons produced by microbial metabolism in the anode zone. The protons were not consumed absolutely in time in the anode or cathode zone (mainly cathode zone). It suggests that the protons utilization was low on the conductive cathode membrane because the probe of pH online detector was placed near the cathode. And carbonates and phosphates with low concentrations, had a weak pH buffering capacity. To improve the performance deterioration, the concentration of NaHCO3 in influent of the reactor R2 increased from 0.3 g L−1 to 0.5 g L−1 at 125 days, 0.7 g L−1 at 138 days, respectively. With the increase of NaHCO3, the pH increased gradually from 6.2 to 6.7 in the supernatant of AnEMBR system up to 143 days. In general, the optimal pH range was 6.5–7.5 for methanogens living. Obviously, pH value was in the optimal pH range for the reactor R2 after 143 days. And difference of pH values was <0.2 between two reactors at the same point in time during the whole operation, except when the reactor R2 broke down. It suggests that higher alkalinity could prevent the AnEMBR system from acidification. It is necessary to make an additional cost to ensure the AnEMBR system operation for a long time, due to an increase in the alkalinity demand, compared with the AnMBR system. This was an important and different factor for the long-running AnEMBR system, compared with the short-running AnEMBR system.
Fig. 2 COD removal during the whole operation of the reactors R1 and R2 (a) and (b). Physical diagram of R1 (c) and R2 (d) before operation. Physical diagram of R1 (e) and R2 (f) under operation. |
As is shown in the Fig. 2(b), the COD removal changes were similar between each other before 65 days. COD concentrations in effluent decreased in the first 8 days and increased within 9–21 days. This may be for the reasons that anaerobic microorganisms had to take some time to adopt the new environment for growing and enriching, while initial organic matter in the inoculated sludge from the wastewater treatment plant was to be digested and diluted with replaced tap water. COD concentrations in effluent were relatively high from 8 to 65 days, but declined gradually. It may suggest that a lot of bacteria died and dominant population was too low to digest excess organic matter, but the dominant bacteria was enriching. There was some difference for COD removal in both reactors. The effluent COD concentration was stable at a low level in the reactor R1 after 66 days. But the low and stable COD concentration only existed within 66–110 days when the cathode potential was −0.5 V in the reactor R2. The COD concentration in effluent showed a liner rate of increase from the 110 days to 123 days during the operation of R2 system. Surprisingly, the COD concentration in effluent at 123 days had already been more than that at the first day in the reactor R2. There was little or no biological activity in the R2 system at 123 days. At the same time, the system R2 was examined from head to toe within 13 days. pH values in supernatant of the reactor R2 (6.15–6.35) were lower than those in supernatant of the reactor R1 (6.5–6.6) within 110–123 days, and the pH began to decrease at 100 days. It could be seen that R2 system exhibited a poor self-regulating ability for acidification in the long-term operation, compared with R1 system. So, the concentration of NaHCO3 in influent of the reactor R2 increased from 0.3 g L−1 to 0.5 g L−1 at 125 days. Interestingly, effluent COD concentration decreased rapidly in the reactor R2 during two days. But effluent COD concentration maintained relatively high level and the optimal anaerobic environment was still not be absolutely recovered in the reactor R2 up to 138 days. For better comparative analysis, the concentration of NaHCO3 in influent of the reactor R2 continued to be increased by 0.2 g L−1 and the corresponding pH is 6.5 in the supernatant at 138 days. The pH value was approximate to that in the supernatant of the reactor R1. However, there was no better COD removal than that of the reactor R1.
Furthermore, the average COD concentration was 33.68 mg L−1 in effluent of the reactor R1 during the stable operation. And the average COD concentrations in effluent of the reactor R2 from stage 1 to 3 were 37.79, 64.20 and 39.62 mg L−1, respectively. As shown in Fig. S4 (left),† there was obvious difference for SCOD concentrations in both supernatants. The average SCOD concentration was 57.09 mg L−1 in supernatant of the reactor R1 during the stable operation. But average SCOD concentrations in supernatant of the reactor R2 from stage 1–3 in order were 67.48, 105.09 and 98.51 mg L−1, respectively. Both average COD concentration in influent of the reactors R1 and R2 was 315 mg L−1. So, the biological treatment contribution rate and membrane separation contribution rate of R1 and R2 were 91.68% and 8.32%, respectively. It could be seen that anaerobic digestion process in the system R1 played a major role for treatment of synthetic wastewater. Glucose as a simple organic compound, finally was converted smoothly into methane, hydrogen and carbon dioxide through anaerobic digestion process in the R1 system. In comparison, biological treatment contribution rates of the reactor R2 from stage 1 to 3 were 89.29%, 83.70% and 83.38%, respectively. Membrane separation contribution rates in supernatant of the reactor R2 from stage 1 to 3 were 10.71%, 16.30% and 16.62%, respectively. Obviously, membrane separation contribution rates of the reactor R2 were all higher than that of the reactor R1, but the trend for biological treatment contribution in sludge zone was opposite. It could suggest that the applied voltage had a positive effect on organic degradation or repulsion in the cathode zone, but a negative relatively effect on organic degradation in the anode zone. And it might be attributed to the electrostatic repulsion enhancing the membrane separation. If the biological treatment efficiency had been improved, the transfer velocity of electrons and protons would be a key factor, especially for the large reactors. And the control of alkalinity would be an important and effective way to solve the problem of acidification in the AnEMBR system. Hence, it is important to research the effect of different pH on the AnEMBR system and seek optimal solutions to accelerate the transfer of electrons and protons in the future.
In addition, acetate was the major component of the volatile fatty acids in the supernatant of both reactors (Fig. S4 (right)†). The acetate concentrations in the supernatant of the reactor R2 (8.18, 18.91 and 22.48 mg L−1, from the stage 1 to 3, respectively), were always more than those in the reactor R1 (6.76, 8.21 and 9.28 mg L−1, from the stage 1 to 3, respectively). And the acetate concentrations in effluent presented the same change. The CH4 production produced mainly in the sludge zone of the reactor R1. But less organic matter was oxidated absolutely in the anode while some acetate was converted into CH4 and CO2 on the cathode by the Methanothrix (Fig. S11 and S12†) in the reactor R2. The change of acetate concentration was a reaction of COD and the reasons were the same as the COD removal.
The membrane modules were taken out from the reactors and the macroscopic representation was showed in Fig. S5.† Surprisingly, the colour of cake layers on the membrane surface in the reactors R1, R2 were a little dark green and dark, respectively. It is worth noting that the reactors were shaded by a layer of aluminum foil except for some areas fitted with a gas bag and electrodes on the top of the reactor R2. No green algae appeared in the liquor.
The morphological microstructure on the used membrane surface was showed in the Fig. S6.† A lot of pollutants covered heavily the membrane surfaces with the complicated network structure. And the quantity of micron-size pores on the membrane surface in the reactor R2 was relatively more than that in the reactor R1. By magnification observation, some pores on the membrane surface might be caused by biogas bubbles bursting in the cake layer.
Moreover, the used membranes in the reactors R1, R2, were cut off by the same way. Then the cross-sectional morphologies of the used membranes were taken into scanning electron microscope (SEM) images, as shown in Fig. S7.† The cross-section of a cake layer in the reactor R1 was thick, and prone to being broken easy. In comparison, the cake layer was relatively solid and thin in the reactor R2. These results might be a reaction of different binding force among chemical compositions of cake layers pollutants on the different membrane surfaces. In contrast to the unused membrane surfaces (Fig. S8†), there are less pollutants in the carbon nanotubes mats with negative charges.
Fig. 4 Infrared spectra of the used membranes in the reactors R1 and R2 (left). Infrared spectra of the unused and used membranes in the reactors R1 and R2 (right). |
EEM fluorescence spectroscopy is showed in the Fig. 5. Overall, there were four mainly strong absorption peak in each spectrum, T11, T21, T12 and T22, respectively. These peaks (T11 and T21) were related to tyrosine proteins and others were related to tryptophan proteins.31 And locations and intensities of above absorption peaks are showed in Table S5.† It could be seen that contents of tyrosine and tryptophan proteins on the membrane surface were 1.16 and 1.34 times as much as these on the electro-assisted membrane surface, respectively.
Fig. 5 EEM fluorescence spectroscopy results for the pollutants on the membrane surface in the reactors R1 (left) and R2 (right). |
Moreover, charged cake layers on the membrane surfaces were characterized by zeta potential, as shown in Table S6.† The average zeta potential was −26.77 (±0.27) mV for the pollutants on the membrane surface in the reactor R1, but −22.47 (±0.27) mV in the reactor R2. The sludge in the reactor R2 contained lower negative charges. It should be taken into consideration that negative surface charges increased linearly with the total extracellular polymer (EPS) content in sludge and increased proteinaceous and carbohydrate fractions played a major role in the EPS.32 Therefore, the less proteins or EPS with less negative charges deposited and agglomerated on the electro-assisted membrane. These results about EEM fluorescence spectroscopy and zeta potential were corresponding to the above FTIR analysis.
In addition, different sludge particles formed gradually a cake layer with depositing on membrane surface during filtration. The particle size of sludge is showed in Table S8.† Particle size of >90% particles on the electro-assisted membranes was smaller than that on the membrane without applied voltage. And particle size of >50% particles in the anode zone was smaller than that in the sludge zone. These results were opposite to the traditional experimental conclusion about membrane fouling mechanism in the anaerobic membrane reactor. It is normally regarded that small particles were easier than large particles to block the pores on the membrane surface, resulting in increasing density of cake layers and reducing permeability of the membrane in the membrane reactor.36 Furthermore, the particle size of pollutants on the membrane surface in the reactor R2 was very close to that in the sludge zone of the reactor R1 or R2. And the particle size of pollutants on the membrane surface was the biggest in the reactor R1. The reason might be that, the amounts of microorganisms on the membrane surface in the reactor R2 was more than that in the reactor R1. And there were more abiotic pollutants, including EPS, colloid and salt deposition, on the membrane surface in the reactor R1.
Fig. 6 Potential on anode and cathode and potential difference between anode and cathode (left). The current through the system R2 measured by the electrochemical workstation (right). |
In view of CH4 production, the change of biogas from the system R2 (AnEMBR) was similar to the change of temperature detected by the online monitor. But the biogas production decreased gradually with decreased experimental temperature in the system R1. It is a possible that temperature might seem to have a smaller influence on biogas produced by the system R2 and AnEMBR system seemed to have a potential advantage for the wastewater treatment in the low temperature, for example, in winter.
Furthermore, the main microbial species and proportions were presented at the class and gene levels on the membrane surface of the reactors R1 and R2, in the Fig. S9–S12,† respectively. The proportions of Methanomicrobia group at the class level were 1.78% and 4.49% of the microbial community on the membrane surface of the reactors R1 and R2, respectively. The result explains the CH4 production observed in this study. Anaerolineae and Clostridia groups for degrading soluble organic matter38,39 on the membrane surface of the reactor R2 (5.17% and 8.14%, respectively) were higher than those of the reactor R1 (7.45% and 2.28%, respectively). And the exoelectrogenic bacteria, mainly including Betaproteobacteria, Deltaproteobacteria and Grammaproteobacteria, on the membrane surface of the reactor R2 accounted for 1.96%, 10.98% and 2%. The values were all more than those of the reactor R1 (0.7%, 9.08% and 0.79%, respectively). Furthermore, an acetoclastic methanogen named Methanothrix was the dominant methanogens on the cathode of the reactor R2, accounting for 3.79%. The value was far higher than that on the membrane surface of the reactor R1. Methanothrix could participate in direct electron transfer (DET) to produce CH4 using the CO2 reduction pathway or acetate decarboxylation pathway.40 In addition, the genus Desulfovibrio was an important and dominant sulfate-reducing bacteria community41 on the cathode of the reactor R2 (2.39%). In comparison, the proportion of the genus Desulfovibrio was only 0.85% on the membrane surface of the reactor R1. Some Desulfovibrio species could use directly the electrons and energy from the cathode42 or hydrogen, organic acids, or alcohol.43 And H2 was only utilized when acetate presented.43 The exoelectrogenic bacteria was beneficial for improving bioelectrochemical methane gas production in the system R2.
Footnote |
† Electronic supplementary information (ESI) available. See DOI: 10.1039/d1ra05500c |
This journal is © The Royal Society of Chemistry 2021 |